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Q&A

Comments on Humming noise from a boost converter's inductor

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Humming noise from a boost converter's inductor

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My step-up converter makes audible noise both with and without a load.I am almost certain it is the inductor, because when I hold my finger on it I can feel vibration and it gets quieter. Unfortunately, I do not own an oscilloscope and cannot inspect what is going wrong. Here is the schematic: Image alt text

All the capacitors are ceramic, inductor is FXL0530-100-M, and the converter datasheet can be found here . On page 14, FIGURE 6-8 the recommended values are shown. Only thing I have changed are resistor values to match my output voltage, but this is a minor change. I read about audible issues with converters, and one of the points mentioned was that picking an IC with a higher switching frequency can help, but this particular one is at 1MHz, well above the one mentioned in the article I read.

What could be the reasons for this humming noise, and how could they be mitigated?

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General comments (2 comments)
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First, draw schematics properly when you ask others to look at them. Your right to left flow is rather annoying.

There are two main possibilities for this circuit to cause noise, the inductor and the output capacitor.

Inductor

The inductor can make sound for two reasons:

  1. Every bit of wire is subjected to a sideways force due to the magnetic field. As that changes, the force on the wire changes. The windings aren't meant to move, but small vibrations happen anyway.
  2. The magnetorestrictive effect. Some magnetic materials change size slightly as a function of the magnetic field.

Capacitor

The capacitor can make sound due to the piezoelectric effect. This is the electrical analog of the magnetorestrictive effect. The material changes size slightly as a function of the electric field.

The reverse is also true, meaning the voltage on a ceramic capacitor can change slightly due to applied force. This undesirable property even has a name, called microphonics. This is why ceramic capacitors are usually banned from the signal path of sensitive audio circuits.

4.7 µF for the output cap seems rather small. I didn't read the whole datasheet, but the examples I saw used 10 µF. Maybe it's within specs, but there is certainly no harm in making it higher. That would make the output voltage smoother, which includes less voltage change across the capacitor.

Instability

The above explains why this circuit could make sound at the switching frequency. Since that's 1.2 MHz according to the datasheet, that's clearly not what you're hearing. This is actually a symptom of a worse problem, which is that the controller is not stable.

What is happening is that the controller is going meta-stable. Over a number of pulses, the voltage goes up. This causes the PWM to get cranked back for a number of pulses. The result is oscillation at a lower frequency than the switching frequency. This is what you are hearing. You really should fix that.

I'd try paralleling another capacitor across C1. You don't give any specs on C1, so we don't know the voltage rating. For some ceramic caps, the capacitance drops off significantly with voltage. If this is a 30 V cap, for example, then the capacitance may be significantly less than 4.7 µF at 25 V.

I see now that there is a table on page 12 of the datasheet, which says 4.7 µF is sufficient above 16 V output. That doesn't mean that higher values are bad.

Even though the datasheet only says the chip needs 1 µF input capacitance, there is clearly no reason you can't use more. Surely this part works with a 0 impedance voltage source as input. I'd put 10 µF there since that's cheap and easy.

Voltage step-up ratio

You are asking for a voltage step-up ratio of (25 V)/(5 V) = 5. That requires a nominal PWM duty cycle of 80%. That's close to the maximum duty cycle of 85% this chip is intended for.

Diode

At these voltages and currents, you really should be using a Schottky diode. They have half the forward drop, and are very fast. I didn't look up your diode, but another possible problem is that it has too long of a reverse recovery time. At over 1 MHz switching speed, this is very important. Any ordinary diode is far from good enough here.

Fixes

You may still be in spec, but right at the edge pushing some of the limits. Use a little intuition and try to make it as easy for the chip as possible. Like with most things in life, trying to slide by with the bare minimum gets you in trouble eventually when everything else isn't just right.

Using a bigger input cap is a no-brainer.

Using a Schottky diode is a no-brainer, and in fact the lack thereof may well be causing significant trouble.

Most likely a larger output cap would help. The meta-oscillations are due to control instability. The most likely cause of that is insufficient output capacitance. Your "4.7 µF" cap probably isn't 4.7 µF at 25 V.

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General comments (2 comments)
General comments
Kranulis‭ wrote over 4 years ago

The diode is in fact a schottky with a 500ns recovery time. Both capacitors are rated 50V, both X7R. I replaced input and output capacitors with the same rating 10uF capacitors. The noise is still present, but after touching each component with tweezers, I felt most vibrations from C1 (output). I will try to get a bigger one and see if it helps!

Olin Lathrop‭ wrote over 4 years ago

@Brok: Your schematic shows a normal diode. You need to take more care with your schematics. You are wasting the time of the volunteers that are trying to help you.