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Q&A MAX485 transceivers breaking, Pi filter generating spikes?

Problem description & speculation about causes I've having a problem with MAX485 transceivers breaking intermittently, passing our production tests but later failing. The error phenomenon is w...

2 answers  ·  posted 9mo ago by Lundin‭  ·  last activity 9mo ago by Andy aka‭

Question EMC pi-filter RS-485
#2: Post edited by user avatar Lundin‭ · 2024-03-16T12:04:51Z (9 months ago)
  • **Problem description & speculation about causes**
  • I've having a problem with MAX485 transceivers breaking intermittently, passing our production tests but later failing. The error phenomenon is wrong signal voltage levels on the RS485 lines, as well as the transceiver failing to return the signals to 0V.
  • Switching out Maxim for another brand solves the problem. At first I suspected that we had gotten counterfeit parts, but that starts to seem less likely. Maxim/AD will give no technical support and are unhelpful in general.
  • What's notable is that we for some reason (still investigating why) is using MAX485 ESA instead of MAX485 EESA, the latter having built-in ESD protection diodes (which ought to be standard these days but apparently not). The other brands (TI, Sipex etc) that do not break have built-in protection diodes.
  • But since this design uses external TVS we never considered ESD a problem. The product has undergone ESD testing in a lab with 8kV contact 15kV air and passed. As well as a bunch of other very tough conducted/radiated susceptibility tests. So I'm pretty confident at ruling out ESD during production or product use as the culprit. We can also rule out external transients since some parts failed during production testing.
  • We have noted some spikes of a few volts extra on the edges of the RS-485 data. Nothing extreme - we probably dismissed it as poor scope ground or bad probes:
  • ![Image_alt_text](https://electrical.codidact.com/uploads/ndxudleq4bx8a6hhax4xw2kcoxg2)
  • Baudrate is 50kbps.
  • What we suspect now is that a couple of extra Pi filters with ferrites (far right side of the schematic below), that were added late during a failed EMC test, could somehow create spikes through self-resonance(?) or some manner of EMF(?). Too low for the 33V TVS to kick in, but high enough to kill the MAX485.
  • Since switching to a 2nd source transceiver fixes the problem, the theory is that the protection diodes of the 2nd source part takes care of these small spikes.
  • **Schematic**
  • ![Image_alt_text](https://electrical.codidact.com/uploads/j8v9tbdo4vwxvda115o7x81dnq74)
  • **Datasheets/BoM**:
  • - [IC1 MAX 485](https://www.analog.com/media/en/technical-documentation/data-sheets/MAX1487-MAX491.pdf)
  • - [L1 common mode choke](https://www.murata.com/en-eu/api/pdfdownloadapi?cate=luNoiseSupprFilteChipCommoModeChokeCoil&partno=DLW31SH222SQ2%23)
  • - [L2, L3 ferrite beads](https://www.we-online.com/catalog/datasheet/74275022.pdf)
  • - [D1, D2 Bidirectional TVS 33V 600W peak pulse](https://www.st.com/resource/en/datasheet/sm6t33ca.pdf)
  • - [C1 to C4 MLCC 0603 C0G 50V](https://eu.mouser.com/datasheet/2/281/1/GRM1885C1H470JA01_01A-1984945.pdf)
  • - [C5, C6 MLCC 1210 X7R 500V](https://www.vishay.com/doc?45197)
  • - [C7, C8 MLCC 1206 X7R 250V](https://www.we-online.com/catalog/datasheet/885342208004.pdf)
  • - [R1 1206 1%](https://www.mouser.se/datasheet/2/348/ROHM_S_A0011075102_1-2563252.pdf)
  • **Application description**
  • The application is a 24VDC supply civil product for military use. It has gone through extensive EMC testing against MIL 461G and passed all tests (conducted/radiated emissions, conducted/radiated susceptibility, ESD, power supply tests etc etc). Since this includes a very broad range of noise from 2MHz up to 18GHz somewhere, all EMC counter measures are kept general-purpose.
  • We have 2x the above schematic that forms a point-to-point semi-duplex communication and either side of it is failing. As seen in the schematic, the outer caps of the Pi filter towards the connectors are chassis grounded. PCB ground is connected to chassis but not near the RS-485 lines.
  • Shielded cables are used and distances are approximately 30m. Baudrate 50kbps. We haven't used twisted pair, which would obviously be a sound idea, but passed EMC testing regardless.
  • The 47pF caps are for a bit of slope as well as filtering. The bus is terminated in both ends with 120R for 60R impedance.
  • **Questions**
  • - Are the theories about self-resonance or reverse EMF likely?
  • - Theories about something else be causing the problems?
  • - Might it be counterfeit parts after all? Even though we bought them from a reliable source (although not one of Maxim's favored ones). And this is such a common, well-known part - I've used it many times before in other projects.
  • - Any other design review concerns?
  • The problem is already solved in practice by blacklisting the Maxim parts as well as adding a few smaller TVS suitable for RS-485 signal levels. But I need to find the root cause.
  • **Problem description & speculation about causes**
  • I've having a problem with MAX485 transceivers breaking intermittently, passing our production tests but later failing. The error phenomenon is wrong signal voltage levels on the RS485 lines, as well as the transceiver failing to return the signals to 0V.
  • Switching out Maxim for another brand solves the problem. At first I suspected that we had gotten counterfeit parts, but that starts to seem less likely. Maxim/AD will give no technical support and are unhelpful in general.
  • What's notable is that we for some reason (still investigating why) is using MAX485 ESA instead of MAX485 EESA, the latter having built-in ESD protection diodes (which ought to be standard these days but apparently not). The other brands (TI, Sipex etc) that do not break have built-in protection diodes.
  • But since this design uses external TVS we never considered ESD a problem. The product has undergone ESD testing in a lab with 8kV contact 15kV air and passed. As well as a bunch of other very tough conducted/radiated susceptibility tests. So I'm pretty confident at ruling out ESD during production or product use as the culprit. We can also rule out external transients since some parts failed during production testing.
  • We have noted some spikes of a few volts extra on the edges of the RS-485 data. Nothing extreme - we probably dismissed it as poor scope ground or bad probes:
  • ![Image_alt_text](https://electrical.codidact.com/uploads/ndxudleq4bx8a6hhax4xw2kcoxg2)
  • Baudrate is 50kbps.
  • What we suspect now is that a couple of extra Pi filters with ferrites (far right side of the schematic below), that were added late during a failed EMC test, could somehow create spikes through self-resonance(?) or some manner of EMF(?). Too low for the 33V TVS to kick in, but high enough to kill the MAX485.
  • Since switching to a 2nd source transceiver fixes the problem, the theory is that the protection diodes of the 2nd source part takes care of these small spikes.
  • **Schematic**
  • ![Image_alt_text](https://electrical.codidact.com/uploads/j8v9tbdo4vwxvda115o7x81dnq74)
  • EDIT: D1 and D2 are on different lines, naturally. I messed up while redrawing the schematic.
  • **Datasheets/BoM**:
  • - [IC1 MAX 485](https://www.analog.com/media/en/technical-documentation/data-sheets/MAX1487-MAX491.pdf)
  • - [L1 common mode choke](https://www.murata.com/en-eu/api/pdfdownloadapi?cate=luNoiseSupprFilteChipCommoModeChokeCoil&partno=DLW31SH222SQ2%23)
  • - [L2, L3 ferrite beads](https://www.we-online.com/catalog/datasheet/74275022.pdf)
  • - [D1, D2 Bidirectional TVS 33V 600W peak pulse](https://www.st.com/resource/en/datasheet/sm6t33ca.pdf)
  • - [C1 to C4 MLCC 0603 C0G 50V](https://eu.mouser.com/datasheet/2/281/1/GRM1885C1H470JA01_01A-1984945.pdf)
  • - [C5, C6 MLCC 1210 X7R 500V](https://www.vishay.com/doc?45197)
  • - [C7, C8 MLCC 1206 X7R 250V](https://www.we-online.com/catalog/datasheet/885342208004.pdf)
  • - [R1 1206 1%](https://www.mouser.se/datasheet/2/348/ROHM_S_A0011075102_1-2563252.pdf)
  • **Application description**
  • The application is a 24VDC supply civil product for military use. It has gone through extensive EMC testing against MIL 461G and passed all tests (conducted/radiated emissions, conducted/radiated susceptibility, ESD, power supply tests etc etc). Since this includes a very broad range of noise from 2MHz up to 18GHz somewhere, all EMC counter measures are kept general-purpose.
  • We have 2x the above schematic that forms a point-to-point semi-duplex communication and either side of it is failing. As seen in the schematic, the outer caps of the Pi filter towards the connectors are chassis grounded. PCB ground is connected to chassis but not near the RS-485 lines.
  • Shielded cables are used and distances are approximately 30m. Baudrate 50kbps. We haven't used twisted pair, which would obviously be a sound idea, but passed EMC testing regardless.
  • The 47pF caps are for a bit of slope as well as filtering. The bus is terminated in both ends with 120R for 60R impedance.
  • **Questions**
  • - Are the theories about self-resonance or reverse EMF likely?
  • - Theories about something else be causing the problems?
  • - Might it be counterfeit parts after all? Even though we bought them from a reliable source (although not one of Maxim's favored ones). And this is such a common, well-known part - I've used it many times before in other projects.
  • - Any other design review concerns?
  • The problem is already solved in practice by blacklisting the Maxim parts as well as adding a few smaller TVS suitable for RS-485 signal levels. But I need to find the root cause.
#1: Initial revision by user avatar Lundin‭ · 2024-03-15T12:22:18Z (9 months ago)
MAX485 transceivers breaking, Pi filter generating spikes?
**Problem description & speculation about causes**  
I've having a problem with MAX485 transceivers breaking intermittently, passing our production tests but later failing. The error phenomenon is wrong signal voltage levels on the RS485 lines, as well as the transceiver failing to return the signals to 0V. 

Switching out Maxim for another brand solves the problem. At first I suspected that we had gotten counterfeit parts, but that starts to seem less likely. Maxim/AD will give no technical support and are unhelpful in general.

What's notable is that we for some reason (still investigating why) is using MAX485 ESA instead of MAX485 EESA, the latter having built-in ESD protection diodes (which ought to be standard these days but apparently not). The other brands (TI, Sipex etc) that do not break have built-in protection diodes.

But since this design uses external TVS we never considered ESD a problem. The product has undergone ESD testing in a lab with 8kV contact 15kV air and passed. As well as a bunch of other very tough conducted/radiated susceptibility tests. So I'm pretty confident at ruling out ESD during production or product use as the culprit. We can also rule out external transients since some parts failed during production testing.

We have noted some spikes of a few volts extra on the edges of the RS-485 data. Nothing extreme - we probably dismissed it as poor scope ground or bad probes:

![Image_alt_text](https://electrical.codidact.com/uploads/ndxudleq4bx8a6hhax4xw2kcoxg2)

Baudrate is 50kbps.

What we suspect now is that a couple of extra Pi filters with ferrites (far right side of the schematic below), that were added late during a failed EMC test, could somehow create spikes through self-resonance(?) or some manner of EMF(?). Too low for the 33V TVS to kick in, but high enough to kill the MAX485.

Since switching to a 2nd source transceiver fixes the problem, the theory is that the protection diodes of the 2nd source part takes care of these small spikes.

**Schematic**

![Image_alt_text](https://electrical.codidact.com/uploads/j8v9tbdo4vwxvda115o7x81dnq74)

**Datasheets/BoM**:  
- [IC1 MAX 485](https://www.analog.com/media/en/technical-documentation/data-sheets/MAX1487-MAX491.pdf)
- [L1 common mode choke](https://www.murata.com/en-eu/api/pdfdownloadapi?cate=luNoiseSupprFilteChipCommoModeChokeCoil&partno=DLW31SH222SQ2%23)
- [L2, L3 ferrite beads](https://www.we-online.com/catalog/datasheet/74275022.pdf)
- [D1, D2 Bidirectional TVS 33V 600W peak pulse](https://www.st.com/resource/en/datasheet/sm6t33ca.pdf)
- [C1 to C4 MLCC 0603 C0G 50V](https://eu.mouser.com/datasheet/2/281/1/GRM1885C1H470JA01_01A-1984945.pdf)
- [C5, C6 MLCC 1210 X7R 500V](https://www.vishay.com/doc?45197)
- [C7, C8 MLCC 1206 X7R 250V](https://www.we-online.com/catalog/datasheet/885342208004.pdf)
- [R1 1206 1%](https://www.mouser.se/datasheet/2/348/ROHM_S_A0011075102_1-2563252.pdf)

**Application description**  
The application is a 24VDC supply civil product for military use. It has gone through extensive EMC testing against MIL 461G and passed all tests (conducted/radiated emissions, conducted/radiated susceptibility, ESD, power supply tests etc etc). Since this includes a very broad range of noise from 2MHz up to 18GHz somewhere, all EMC counter measures are kept general-purpose. 

We have 2x the above schematic that forms a point-to-point semi-duplex communication and either side of it is failing. As seen in the schematic, the outer caps of the Pi filter towards the connectors are chassis grounded. PCB ground is connected to chassis but not near the RS-485 lines.

Shielded cables are used and distances are approximately 30m. Baudrate 50kbps. We haven't used twisted pair, which would obviously be a sound idea, but passed EMC testing regardless. 

The 47pF caps are for a bit of slope as well as filtering. The bus is terminated in both ends with 120R for 60R impedance.

**Questions**  
- Are the theories about self-resonance or reverse EMF likely? 
- Theories about something else be causing the problems? 
- Might it be counterfeit parts after all? Even though we bought them from a reliable source (although not one of Maxim's favored ones). And this is such a common, well-known part - I've used it many times before in other projects.
- Any other design review concerns?

The problem is already solved in practice by blacklisting the Maxim parts as well as adding a few smaller TVS suitable for RS-485 signal levels. But I need to find the root cause.